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Flow meter set & continuosly observing. ( Why coolant stops)
ELB Rim
Cycle running time coolant not coming
Emergency pressed by operator, so released switch then ok.
Assembly station 1
Cun not running
Machine abnormal error reset done, then trial found ok.
Nissin
Machine cycle not starting
Filter cleaned
Test Rig F1 & F2
PT line filter pressure high & hydraulic oil temperature high
Utility side conpressor tripped, so temperature rised. Trip recovered then temperature decreased. Then handed over to production.
ELB Rim
Chiller temperature high
Utility side conpressor tripped, so temperature rised. Trip recovered then temperature decreased. Then handed over to production.
Micromatic Grinding
Chiller unit fault
All sensors cleaned then cycle started. No alarm coming
Stahli S/F Grinding Machine 2
Protection hood mechanically off
Interchanged scanner with jerk test machine ( Ramesh sir's instraction )
PV Assembly & Leak Testing
Scanner not working
Checked reed switch position, adjusted it then pallet present sensor removed & cleaned & machine restart.
Centre Lapping
Cobot not operate & conveyor pallet not stop
Checked input 73.1 & another input found ok then checked coil resistance, found ok. Need to check further.
ELB Rim
Coolant off in running cycle
Pumping process done, then added deformer
Durr Ultrasonic
Work tank to FT.1 time exceed
Checked for leakages & valves then interchanged flow meter with Test stand A, but problem not solved. Then only flow meter again interchanged with original flow meter of machine.
Test Rig F2
Slipage variation
Work chamber alignment in center & manually recovered.
Durr Ultrasonic
Basket stuck in work chamber
Work chamber cleaned then added deformber in water & maintaned water level in tank
Durr Ultrasonic
FT 2 to work tank fill time exceeded and oil separator over. Full alarm
Manually recovered
Durr Ultrasonic
Base positioning not done.
Checked all rails & adjusted, but problem not solved so marked pallet and faulty pallet removed
Centre Lapping
Pallet stuck
Checked clamping sensor set machine ok.
Centre Lapping
Pallet clamp problem
SO unloading job removed & machine properhome position done. Machine ok.
Cleantech
Home position problem
PLC restart then machine ok.
Dust Seal
Belt absent problem
Found without job cycle started by operator, so job holding tool not recovering. So manually recovered
Deburring Machine
Without job cycle machine started. ( Operator mistake )
Removed manually
Durr Ultrasonic
Basket stuck up. Conveyor stuck
Manually set the sensors then conveyor moving properly,
Centre Lapping
Conveyor sensor problem
Manually set the sensors then sensor connection problem solved.
Assembly stations of CH01
Ball not present alarm
Manually done the movement
Kadia
Filter paper not moving
Found that the return line filter stuck, then cleaning done
Test Rig G2
Oil over flow
Manually done the declamping
Cleantech
Job declamp problem
New sensor fitting work done
Stahli S/F Grinding Machine 2
Sensor wire broken
Manually tightened the sensor then setting properly done,
Assembly stations of CH02
Sensor loose problem
Dismentaled all hydraulic lines then retightened then pipes with seal, so out 0f 12, 5 nos done, then other handover to 2nd Shift.
BVLINE PVG Test Stand
Oil leakage problem
Interchanged the sensors then properly alignment done of sensors after that restarted the machine.
Test Rig G2
Door sensor not working
Changing one connection just lock the line and dismentaled that line
Studer
Pneumatic connections change
Machine running continue with observation, found coolant tank side pressure gauge variable 8 am to 12 PM, 12 Bar pressure 12PM to 3 PM - 9 Bar pressure
ELB Rim
Coolnat flow problem
Original handle fitted & trial taken OK. (SS-03 Klein machine Original handle )
Klein 1
Original handle fitting work
Found ball feeder cycle not completed, ball feeder cycle complete then problem solved.
Assembly stations of CH02
Spool set clamping problem
When machine started tehn same noise came, need to chaked further( X Axis motro interchanged )
Studer 1 (450)
Noise came from X axis
Checked al reed switch position & sensor trial taken found ok.
Centre Lapping
Cobot stuck
Checked all emergency switch & reset switch & interchanged relay
Test Rig D2
Drain motor not operate & not rotate in two direction
Changed set up &
Assembly stations of CH03
Set up
Checked door alignment and machine restarted
Test Rig G1 & G2
Door locking problem
Checked sensors, found that some time not setting, so cleaned it
Studer
Pallet not stop
Found that oil stuck in proxy cable so cleaned the sensor
Studer
Two conveyor stuck
Manually basket removed & then again shift
Durr Ultrasonic
Basket not going properly
Sensor adjusted &
Studer 1 (450)
Pallet stuck
Checked all sensors working manually and then locking sensors reed switch adjusted
Deburring Machine
Cycle continuosly run
adjusted sensors
Assembly stations of CH01
Ball not came alarm
Checked all conditions then checked photo sensors
Assembly stations of CH04
Conveyor not operate
Coolant pump fitted and rotation checked
Studer
Coolant pump fitted
Return line filter cleanned
Test Rig H1 & H2
Tank pressure high
Topup done 55 Liter,
BVLINE Test Stand A (Single stage)
Hydraulic oil level low
Topup done 1 Liter,
Kadia
Lubrication oil level Low
Pressure regulator installation done.
Test Rig F2
Pressure regulator to be installed
Pressure regulator installation done.
Test Rig G1
Pressure regulator to be installed
Pressure regulator installation done.
Test Rig G2
Pressure regulator to be installed
Manually recovered
Studer 1 (450)
Pallet stuck
Manually recovered
Cleantech
Conveyor over travel and unload problem
Water topup done
Durr Ultrasonic
FT 1 Water level low alarm
Setup changing done
Test Rig E1 & E2
Setup to be changed
SO manually base position set
Durr Ultrasonic
Basket stuck
Gun replaced
Test Rig B
Capping gun faulty
Found basket manually recovered & base psoitioning done,
Durr Ultrasonic
Basket stuck
Found tank pressure filter choked, so cleaned filter
Test Rig H2
Tank pressure high/low alarm came
Hydarulic pressure manually decreased to 39bar.
BVLINE PVM Assembly
Hydraulic pressure setting
Oil top-up done.
Test Rig D1
Oil level low
Oil top-up done.
Cleantech
Lubrication oil level low
Tank line filter cleaning done.
Test Rig F1
Tank pressure low
Checked & machine proper home positioning done.
Cleantech
Cycle not start
Found transfer basket in not going to forward & reverse because work chamber not at home position. So manually homing done. But machine under maintenance. Pending
Durr Ultrasonic
Transfer not goinf to Forward & Reverse
New pipe fitting done.
Stahli S/F Grinding Machine 1
Air pipe leakage
Machine restarted
ELB Wheel
VDI signal problem
Caping gun adjusted
Test Rig F2
Caping Gun problem
Sensor setting done.
Assembly stations of CH01
Poka Yoka not working
PC restarted
Assembly stations of CH01
Software problem
Accorning to checksheets PM Done
Test Rig G1 & G2
Monthly & other PM activity
Accorning to checksheets PM Done
Studer
Monthly & other PM activity
Accorning to checksheets PM Done
Test Rig D
Monthly & other PM activity
Accorning to checksheets PM Done
Test Rig F1 & F2
Monthly & other PM activity
Electrical points completed. ( Pending )
Test Rig G1 & G2
Monthly & other PM activity
Completed PM points as per date.
Studer
Monthly & other PM activity
Completed PM points as per date.
Studer 1 (450)
Monthly & other PM activity
Pending points completed.
Cleantech
Monthly & other PM activity
Found motor taking 2.0 A current & overload realy set to 1.8 A. So set relay on 2.4 A, after that motor not tripping till 11:30 PM.
ELB Wheel
Coolant off problem
All PM completed & some electrial PM points pending earlier also completed.
Studer
M/Q/HY/Y PM activity
All PM completed & some electrial PM points pending earlier also completed.
Studer
M/Q/HY/Y PM activity
All PM completed & some electrial PM points pending earlier also completed.
TOOL ROOM Tshudin
M/Q/HY/Y PM activity
All PM completed & some electrial PM points pending earlier also completed.
Test Rig D
M/Q/HY/Y PM activity
Checked at Hydraulic valve replaced then trial taken ok. 2-3 hydraulic vale replaced.
Test Rig F2
Slipage QT variation problem
Portable chiller hose pipe removed and electrical connection removed. Then kept on place
Studer
Portable Chiller removed and kept on place.
New filter paper provided,
Nissin
Collant filter choke
New filter paper provided,
Cleantech
Filter paper empty
Machine restarted
Test Rig G1
Door locking problem
replaced flow meter
Test Rig C
QCF flow meter replaced
Maintenance QE reset done with maintenance key
Kadia 40
Maintenance QE full
Found LAN cable problem, so reconnected cable & PC restarted,
Assembly stations of CH02
Software problem
Broken basket temporarily tightened with cable tie.
Durr Ultrasonic
Basket stuck
Both mahcine's hydarulic filters cleaning done.
Test Rig G1 & G2
Pressure high/low alarm come
Found M-6 bolt is slipping, so new bolt fitting done,
Test Rig H1
Caping gun height not properly set
Found relay faulty, so replaced relay
Test Rig H2
Motor not rotating in reverse direction
SO removed trip &
Durr Ultrasonic
Transfer con trip
Pound 24 Volt DC supply coming properly, but light not working. And checked and spare light not available. So removed light from machine and kept in department.
Studer 1 (450)
Light not working
Found conveyor stuck, so reset done.
Studer
Job conveyor not working