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Taking in job mode and movement all axis after that trial taken in auto cycle machine working. Okay
Kapp Wheel
X- axis problem
Checked and found gun Bolt missing so fitted new Bolt. ,
BVLINE ECO 80 Assembly
Screw tighting gun problem
Waterline filter cleaning done.
Nissin
temperature problem
Manually separated the water from tank 2.
Durr Ultrasonic
Tank 2 exceed
Clutch assembly dismantled then tightening done.
Test Rig D2
RPM problem
Found flow control is ok, but the single acting valve not working because of leakage. So new valve fitting done.
Cleantech
Cylinder not operating proeprly
Tightned the valve , then no leakage found.
Nissin
Leakage from filter
Model not subdriving so changed the model.
Test Rig G1
Neutral problem
Found that the valve not operate properly. So new valve fitting done.
Test Rig F2
Servo fault
Torque gun reverse forward section jammed. So not able to use. change it with new one fitting done
Test Rig E2
Torque gun problem
Manually released the job. Then found that the hydraulic is not on. So manually turned on
Jerk Testing
Job clamping stack problems.
Manually setting the sensors.
Assembly stations of CH04
Dust seal sensor problem
Fixture mounting disturbed. So need to plan it to proper mounting new plate and bolts fitting .
Assembly stations of CH02
Spool set fixture notch problem
Cleaning the suction filter
Test Rig C
Oil overflow problem
Setting the sensor manually done,
BVLINE ECO 80 Test Stand
Job pressure sensor problem.
Manually restart the machine. Then reset the fault.
Test Rig G2
Door sensor problem
After observation found the X axis motor from kapp rim and fitted on kapp wheel. After interchanging the motor alarm shifted after as it is, and Rim machine handover to production. Wheel X axis motor removed and kept in maintenance room.
Kapp Wheel
003 Alarm coming
F2 Tubelight connection done. F1 pending.
Test Rig F1 & F2
Tubelight reverse
sensor setting properly
Centre Lapping
Sensor problem
Increased the pressure manually.
PV Assembly & Leak Testing
Pressure problem.
Manually operate the sensor setting done.
BVLINE ECO 80 Assembly
Temperature increase problem
Loosen mounting bolts and alignment done properly.
Bolt torquing (Assembly Station)
Pin bolt stuck-up
PLC MCB off &
Test Rig C
PLC communication scanner problem.
Found that wrong model master , That's why happened.
Bolt torquing (Assembly Station)
Torque gun not fitted.
Changed start button box
BVLINE ECO 80 Assembly
Start button damaged found.
Torque setting done.
Durr Ultrasonic
Torquing gun not getting proper torque
Photosensor cleaning done.
Studer
Door not open alarm came.
Found that cobot job not decline so manually declamped it.
Cleantech
Machine not at home position came.
Pressure set as per range.
PV Assembly & Leak Testing
Pressure set as per range.
Two side wire ropes safety door fitted. One side lock not present.
Studer
Door rope not working.
Bush changed
Assembly stations of CH04
Job not ok alarm came.
Safety curtain was disturbed so adjusted it.
Deburring Machine
Cycle not start
Adjusted height
Test Rig F2
Cap Torquin height problem.
So checked and found dust seal sensor setting done
Assembly station 2
Dust seal not present
HMI restart
Assembly station 3
Hmi software is hanging
as Production recruitment sensor removed.
BVLINE ECO 80 Test Stand
Job present sensor removing work
Checked and found Convoyer MCB trip. So removed trip
Durr Ultrasonic
Conveyer not start
Found pilot filter chocked so removed filter and new filter fitting done
Test Rig F2
Imbalance DPS and QP DPS value variation
Found new M5 nut & bolt fitting done.
Durr Ultrasonic
Convoyer stopper mounting remove.
According to production team proximity referencing done and setting done
Kapp Rim
Proximity malfunctioning.
Checked and found the temperature increasing done. So we are checked the temperature sensor and cleaning done
ELB Rim
Temperature issue
So oil cap removed and cleaning done.
ELB Rim
Tellus oil cap not clean.
Checked and found station 2 software issue, so machine restarted,
Assembly stations of CH02
Station two scanner not working.
Remote cap and properly cleaning done. Then refitting done
ELB Rim
Tellus v-15 oil tank cap cleaning work.
Safety curtain position was disturbed so aligned properly
Assembly station 4
Safety cutain checking.
Checked and found the PC power supply is not coming. So Switched the socket of supply.
BVLINE Test Stand A(Dual stage)
PC not working.
Found the clamping fixture is not fixed properly. So clamping fixture tightening done.
Test Rig A
Clamping fixture is not working.
Tube light connection done as per production recruitment.
Test Rig F1
Tube light connection issue
Pressure setting done
Piston Coining
Pressure problem.
Checked & new dauty washer fitting done, then oil top-up done. No leakage currently.
BVLINE PVG Test Stand
Oil leakage problem
PC restarted.
PDI Assembly & PDI Packing CH01 Line 1
PC on turning on.
Sensor damaged so faulty sensor replaced with new one
Dust Seal
Ball absent sensor not working
Socket fixed by Fevi-quick.
BVLINE PVG Test Stand
connection socket damaged
Found many problems are there. so, at first, changed 5 nos of relays. Then found that LAN cable problem. Then changed the extension board. New board fitting done. Then New LAN cable fitting done. Then finally, problems solved. Trial taken ok
Test Rig B
Oil overflow from seal
Air pressure was too high so one flow controller fitting done and adjusted flow
Test Rig E2
Torque gun air flowing problem.
Founded sensor hangs so restarted the total machine, Problem solved.
Test Rig G2
Door sensor problem
Manually setting the gun height and torque done
Test Rig F1 & F2
Torque gun height and torque problem.
Top up done of lubrication oil
Cleantech
Lubrication oil level low.
After inspection found that the oil leakage from the telescope below cover. so after opening the bellow cover, we found that the oil is not draining because of the drain hole is jammed by sludge. So after cleaning all the drain points, we cover the below cover and fitting with sealant so that leakage not happen Then handover machine to production. M/C Under observation
ELB Rim
Oil leakage problem
We found that the key stuck with cover. So the key recovered by lossing bolts and it not working. So after setting it properly
Studer
Door not close problem
Safety door properly not locking because of alignment disturbed so properly alignment done.
Test Rig G2
Safety door properly not locking at cycle time.
Checked & found brush shaft not fitted properly. So new grub screw fitted and properly tightened.
Deburring Machine
Small brush not moving
Checked clamping sensors are disturbed and one sensor damaged. So new sensor fitted and properly setting done
Test Rig B
Job clamp declamp problem.
Spline shaft grub screw properly tightened
Test Rig G2
Spline shaft loose.
Checked and found drive error. So error reset.
Studer
Cobot stuck
Checked and found safety curtain alignment disrupts so properly fitting done.
BVLINE PVM Assembly
Safety curtain problem.
Checked index degree cable cut so rejoined the cable. favourite machine lower cylinder not forwarding so we checked inputs found okay, but yet machine restart S33 machine door open close signal missing so again machine restarted.
Studer
Cobot stuck
So checked and pressure line filter cleaning done
BVLINE ECO 80 Test Stand
Pressure filter choked
New M4 bolt fitting done.
Assembly station 2
Spool fitting assembly cylinder guard bolt missing
Checked and found door position disturb, clips Bolt missing. So new Bolt properly fitted
Test Rig B
Door not closing properly
All nozzle removed and cleaning done. Then fitted properly.
Cleantech
Nozzle cleaning work
Checked & found fixture bolt properly tightening done.
Assembly station 2
Fixture bolt loose
DPPS Line valve Faulty, so replaced valve.
Test Rig F2
Imbalance DPPS bar pressure not achived
Checked and found sensored not working so adjsuted sensor properly.
Assembly stations of CH04
Clamping and declamping problem
Checked and found float switch not working, so fitted new float switch. Then trial taken, but machine not running. So under observation, handover to second shift.
Kadia 40
Float switch problem
Checked and found door not opening during cycle end time. So manually door opened after .
Studer Favorit
Door problem
Homing position problem found over troubled. So set limit switch
Deburring Machine
Over trouble problem.
Checked & found temperature problem. so manually recovered
Test Rig F1 & F2
Temperature problems
Clamping gripper sensor changed
Nissin
Clamping problem.
SO nozzle set machine ok.
Cleantech
Job not cleaning properly.
Sensor cleaning done
Stahli S/F Grinding Machine 2
Protection hood problem
Replaced with F1, F2 interchanged the pumps. Trial pending.
Test Rig E1 & E2
Shock valve pump problem.
Replaced with E1 E2 interchanged the pumps.
Test Rig F1 & F2
Shock valve pump problem.
Manually job declamping done.
Cleantech
Unloading clamping problem.
Manually setting the pressure
Piston Coining
Pressure setting problem
Manually adjusted the sensor.
Test Rig D1
sensor setting problem.
filter cleaning done
Test Rig F1 & F2
Tank pressure high.
Manually set the pressure.
Piston Coining
Pressure setting problem
Manually released the trip.
Cleantech
Spray pump trip problem.
Changing the shaft with new one, fitting down.
Test Rig C
Shaft twist problem.
Using new bolts retightened the sensors.
Stahli S/F Grinding Machine 2
sensor lose
Manually controlled the door opening.
Cleantech
Loading side door not open.
Ngc reset done.
ELB Rim
Cycle not a start.
Cleaning done the scanner then restarted the machine.
PDI Assembly & PDI Packing CH01 Line 1
Scanner not working.
Manually done the unloading.
Cleantech
Unloading problem
All sensor cleaning done. Then trial taken but problem is repeating again and again.
Stahli S/F Grinding Machine 2
Protection hood problem
Manually setting the height of torque Gun
Test Rig G2
Torque gun height problem.
Manually set the pressure.
PV Assembly & Leak Testing
Pressure adjustment problem
Found drain motor mounting is loose so bolts properly tightened.
Test Rig H2
Drain motor mounting loose
Old hose pipe removed and new pipe fitted.
Test Rig F2
Hosepipe fiting work