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Show cut filter paper and manually rotating done
Cleantech
filter paper stocked in rotating wheel
Found PLC error coming so reseted error
Assembly station 3
V-port module not running.
Found manually declamped job.
Test Rig A
The job not declamp
Found the E1, E2 & F1,F2 valves interchanged in shift A so trial taken then machine handovered to production team.
Test Rig E1
Trial pending
Found the coolant is not coming because coolant filter was choked . All 14 nos coolant filter removed and replacement done.
ELB Rim
Coolant is not coming
Checked and found cleantech machine conveyor is not working. Then we manually forward/reversed movement of conveyor
Cleantech
Conveyer not working
Checked and found the spray pump resistance is okay but contractor single phase So we changed conductor. Ah,
Cleantech
Spray pump is not working
Found coolant flow fault so found filtered jam so changed filter
ELB Wheel
Coolant flow fault problem.
Found coolant flow fault so found filter jam so changed filter after that machine ok.
ELB Rim
Spindle motor flow switch fault
Checked and found sensor not working so adjusted sensor
Kapp Rim
Door problem.
Checked and found clutch assembly bolt loose. So tightened properly.
Test Rig H1
Neutral problem.
Checked and found sensored not working so adjusted sensor
Assembly stations of CH03
Bolt torquing problem.
Checked and found Kobot stuck & not working. So manually recovered.
Cleantech
Cobot not working.
Checked and found left hand side door push button damaged. So replaced with new button
BVLINE PVG Assembly
Push button damage.
Checked and found temperature increasing, so manually recovered.
Test Rig D
Temperature problem.
Machine not working because of homing problems. so job removed from plate after that machine taken to home position
Kadia
Homing problem
Motor protection behind sensor changed and teaching done.
Stahli S/F Grinding Machine 1
Motor protection sensor changed
Cheek and found torque problem So adjusted torque
Test Rig G2
Bolt torquing gun problem.
Replaced job present sensor
Piston Coining
Job present sensor faulty
Checked & found that tool is bend, so supervisor says changed later.
BVLINE ECO 80 Test Stand
Tool not fiting in job
Wheel off & pressed door and Also checked alignment.
Studer
Door not open alarm came.
Pressure set manually
Piston Coining
Pressure problem.
Removed PIN & fitted M3 nut bolt
Test Rig F1
Bolt broken
Adjusted height &
Test Rig F2
Torque gun height problem.
Broken stud replaced with new one.
Test Rig A
Stud broken
So sensor setting done properly
Dust Seal
Dust seal not properly fitting
Manually pressure setting done.
Piston Coining
Pressure problem.
Set up changing done.
Test Rig E1 & E2
Set up change.
Coupling properly tightened
Test Rig H1
Spline shaft noise.
Manually homing and the clamp first
Cobot of Studer
Protective alarm came.
Checked AC incoming supply found ok, but E 2 .1. PLC IP not on. So temporarily bypassed
Stahli S/F Grinding Machine 2
Panel AC A01 & A17 alarm came.
Found that PT 100 sensor not properly deep so adjusted sensor
Test Rig D
Temperature problem
Adjusted sensor and changed pallet script, which is stuck
Studer 1 (450)
Pallet stuck
Manually recovered
Cleantech
Unloading time abort alarm game
Manually released water from filtered. Then found temperature little bit decreased But then increased again then found that oil level is low. So top up the oil then checking sensors. But temperature uptown happens. So problem pending
Test Rig D
Temperature problem.
Adjusted the sensors, then found that the alignment of the stopper is not okay. So corrections made to the alignment done. Then again, clean up and setting of the sensor done.
Centre Lapping
Sensor problem.
Fixture setting manually and properly
PDI Assembly & PDI Packing Line 2
Bolt torquing issue.
So cleaning the filter, then refitting it
Test Rig F1
Pressure not increase.
Manually restarted the machine & released alarm. Then restart the machine again
Kadia
Homing problem.
Manaually restarted the cobot, then found the feed is high. Then manually lowered the feed & restarted.
Studer
Cobot stuck.
Manually done the tank operation, then base positioning done. Then problem solved & cycle started in Automode.
Durr Ultrasonic
Cycle start problem.
Top-up done 30 litres bondrite oil given to EMAG Machine.
EMAG Rim
Oil not available.
Checked & found temperature goes 23 degrees & found utility side problem. Told them, and they corrected the temperature
Stahli S/F Grinding Machine 1
Temperature problem.
Checked and found some jobs burning issue due to coolant not fall properly on job. Adjusted coolant nozzle
ELB Wheel
Job burning problem
Checked then found baskets not going properly in auto mode so taken manually and basket entered properly.
Durr Ultrasonic
Basket stuck problem.
Checked & found tank 1 filter clogged ,so replaced with new filter.
Durr Ultrasonic
Tank 1 filter clogged.
Checked & found pc not start because CPU is not on, so turned on CPU then started pc .
Store Punching Machine 1
PC not start.
Found barcode problem, so printed new barcode & provided,
BVLINE PVG Test Stand
Scanner not working
Checked and found pressure not set as per job recruitment. So pressure setting done
Piston Coining
Hydraulic pressure problem
Cleaned sensor
Stahli S/F Grinding Machine 1
Protection hood alarm.
Checked & found RHS port pressure not developed problem.
BVLINE Assembly Station(Single Stage)
RHS port pressure problem
Found stud broken, so replacement work not completed, Handovered to 2nd shift.
Test Rig H1
Stud broken
Check and found motor spline shaft grub screw loose. So tightened properly.
BVLINE ECO 80 Test Stand
Motor spline shaft problem
Job present sensor malfunctioning sensor replacement done
Cleantech
Lifter falling problem.
Heat exchanger line filter jam so filter cleaning done.
ELB Wheel
Oil temperature high 26.5 degree
Capping gun pneumatic straight connector fitting done. For trial operator required.
Test Rig G1 & G2
Capping gun pneumatic connector replaced
Restarted machine .
Test Rig G2
Door not open & not declamp
Manaully declamped
Test Rig G2
Declamp issue
Changed bolts
Test Rig G1
Axis bolt is broken
New machine trial taken, which is 10A load. So trip recovered
PDI Assembly & PDI Packing CH01 Line 1
MCB tripped
Return line filter cleanned
Test Rig C
Tank pressure problem
Cleaned sensors
Stahli S/F Grinding Machine 2
Cycle start problem.
CHecked door alignment and then restarted machine. Problem not solved so removed connector then reconnected them
Test Rig F2
Door locking problem
Proper alignment of switch done
Test Rig E2
Door open problem came
Set clamping force
Studer 2 (451)
Job not declamping properly.
Manually collected
Cleantech
Job fall
Checked belt, then removed assembly found that bearing not moving properly So changed bearing and belt, then fitted properly
Stahli S/F Grinding Machine 1
Vibration coming from cooling unit.
Checked and found alignment problems so properly alignment done.
Stahli S/F Grinding Machine 1
filter motor 2 trip.
Found emergency switch pressed on coolant panel removed emergency
Studer 1 (450)
Coolant flow fault.
Checked & found job holding fixture damaged , so tighten properly
Centre Lapping
Job isn't clamping properly
Manually recovered
Bolt torquing (Assembly Station)
Clamping problem.
Checked & found element fixed on wrong place, so proper placing done.
Cleantech
Cobot's auto cycle, not working
When visited at location, no problem found.
Assembly stations of CH03
Hooter on without any reason.
Checked and found machine on hard limit. So manually recovered.
Assembly stations of CH02
Auto cycle stuck
After opening the cover using Allen key then found a job and returned it to operator. Then more trial taken, but no more falling happening .
Cleantech
Jobs falling.
Checked & found the air leakage, then cut the pipe and rejoined.
Stahli S/F Grinding Machine 1
Air leakage problem.
They don’t give us new mouse. So due to that mouse is damaged, they said that changed it with E1. So E1 machine's mouse fitted to E-2 done. Now, E1 machine don’t have any mouse.
Test Rig E2
Mouse not working
manually opened the door then Released the alarm then auto mode turned on.
Cleantech
Unloading side door stuck.
Sensors cleaning done
Stahli S/F Grinding Machine 2
Protection hood alarm
All points closed.
Test Rig B
Monthly / Q/HY/ Yearly PM activity
All points closed.
Knoll Coolant System
Monthly / Q/HY/ Yearly PM activity
All points closed.
Knoll Coolant System
Monthly / Q/HY/ Yearly PM activity
All pm completed as per check sheet and all pneumatic pipe and cable routing done. Extra cable and pipe removing done nozzle Properly cleaning done.
Cleantech
Monthly / Q/HY/ Yearly PM activity
Pm competed as per cheque sheet
Studer
Monthly / Q/HY/ Yearly PM activity
PM completed as per checksheet and belt is broken Condition, so replaced the belt.
Deburring Machine
Monthly / Q/HY/ Yearly PM activity
So checked temperature sensor PT100 interchanged with Kapp wheel, but still same problem. So interchanged controller with Kapp wheel now machine under observation.
Kapp Rim
Chiller malfunctioning coolant side.
So PM done as part checksheet points
Store Punching Machine 1
Monthly PM need to be done.
So PM done as part checksheet points
Piston Coining
Monthly PM need to be done.
So PM done as part checksheet points
BVLINE ECO 80 Test Stand
Monthly PM need to be done.
All electrical points closed.
Studer Favorit
Monthly PM need to be done.
All electrical points closed.
Nissin
Monthly PM need to be done.
All electrical points closed.
Kadia
Monthly PM need to be done.
All electrical points closed.
Cleantech
Monthly PM need to be done.
Some remaining PM from A shift completed & some pending.
Kapp Rim
Monthly / Q/HY/ Yearly PM activity
PC connection done to UPS supply.
Teijo
PC connection work
Checked & found the temperature controller unit setting done and again to 1 reedy board connector changed then controller setting done Machine handover to production team
EMAG Rim & Wheel
Temperature not proper.
Checked & found the timing belt is broken because bearing and bush was damaged. And one proximity timing belt is faulty so fitted new proximity sensor. Replacement taken and begin trial is ok machine handover to production.
ELB Rim
Timing belt broken again and again.
So checked and found PM completed as per checksheet.
Test Rig H1 & H2
PM activity
So checked and found PM completed as per checksheet.
Deburring Machine
PM activity
All nozzles are cleaned, then refitting done
Cleantech
Nozzle cleaning work