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Cobot restarted. | EMAG Rim | Kobot homing problem. |
sensor properly positioning d1 | EMAG Wheel | Pellet load unload side present sensor position missing. |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | ELB Wheel | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | EMAG Wheel | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | Cleantech | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | Durr Ultrasonic | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | Durr Ultrasonic | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | Assembly stations of CH06 | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | Studer 2 (451) | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | BVLINE PVM Assembly | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | BVLINE PVM Test Stand | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | BVLINE Nitrogen Gas Generator Unit | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | Store Laser Punching Machine 1 | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | Klein 2 | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | Klein 1 | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | Studer | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | ELB Rim | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | ELB Rim | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | Knoll Coolant System | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | EMAG Wheel | PM Activity |
Loose connection found so tightened all connections | Teijo | Rotation trip alarm came. |
Adjusted switch | ELB Rim | Door problem |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | Cleantech | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | Cleantech | PM Activity |
Monthly, Quarterly, Half yearly & yearly PM d1 as per checksheets | Piston Coining | PM Activity |
Changed motor | Test Rig G1 & G2 | Drain Motor replaced activity |
Property mounting d1 | BVLINE Assembly Station(Single Stage) | Wall mounting problem |
New CJC filter fitting d1 both F1 and F2 | Test Rig F1 & F2 | CJC filter replacement |
Motor plate fitted, spindle housing fitted, spindle cooling and air pipe fitted with service engineer. (Alignment pending) new motor wire connection d1 and machine on backup taken by service persons. | EMAG Rim | Linear motor installation work |
Changing d1 and given supply. | Emag China | Chiller unit removed |
Removed accumulator and fitted seal and make Teflon properly trial Due to so handover to night shift person. Observed leakage | Assembly stations of CH04 | Accumulator problem. |
Changed DC unit and given supply. Trial pending due to operator not available. | Studer 2 (451) | DC unit problem. |
Drain motor replaced. | Jerk Testing | Drain motor to be replaced |
Drain motor replaced. | Micromatic Grinding | Drain motor to be replaced |
Drain motor replaced. | KLEIN 3 | Drain motor to be replaced |
Drain motor replaced. | BVLINE Test Stand A (Single stage) | Drain motor to be replaced |
Drain motor replaced. | BVLINE Test Stand B (Single stage) | Drain motor to be replaced |
Checked thoroughly, but no leakage found. | Assembly stations of CH04 | Accumulated leakage need to check. |
filter retightened | Durr Ultrasonic | Vacuum pump oil leakage from filter |
Valve retightened | Assembly stations of CH06 | Valve lose of Air Dryer. |
Pneumatic pipe dressed | Studer | Pneumatic pipe need to be dressed. |
Top cover fitted | EMAG Rim | Top cover to be fitted |
Knob provided. | Studer | Knob to be provided on FRL unit. |
Job removed and again placed then wheel on | Studer Favorit | Wheel not on |
Checked all incoming supply and then interchange power cable, then fitted again and turned on power button | Studer | Guage not operating |
Checked and then found that limit switch plug not proper so connected them properly | Studer | Door open alarm came. |
Compressor LP and HP reset, but problem not solved, then controller reset. | Studer | Compressor temperature high alarm. |
Machine restarted. | Deburring Machine | Cycle not start. |
Incoming supply of conveyor was not coming from main supply switched on. | BVLINE Assembly Station(Dual Stage) | Conveyer not start. |
Changed photos sensor | Studer | Cycle not to start |
Checked valve operating normally and then checked coil found ok. Then checked all pneumatic pipes. Then found that 1 tube pinched, normalized that | BVLINE Assembly Station(Single Stage) | Air leak not operate. |
Manually recovered | Cleantech | Door not operating properly X24 alarm came |
Checked all incoming supply then disconnected capacitor. But motor heating So connected capacitor and trial taken found ok, but need to check further. | Jerk Testing | Drain motor tripped. |
Leakage motor removed and spear motor fitted and leakage test ok. | EMAG Rim | Leakage linear motor removed and spare motor fitted work. |
System restarted and provided 6*6 PU fitting on leakage point. | BVLINE PVG Test Stand | Air leak not okay and system hang. |
Found side cylinders reed switch not on. Slow movement of piston so new flow control provided. | Cleantech | Cycle not start |
Hydraulic pressure adjusted. | Piston Coining | Door not open. |
Manually recovered. | Studer 1 (450) | Component stuck in head and tail stuck. |
Found MPCB trip so released and. | Studer | Mist collected not work. |
Machine trays water drained by pump | Cleantech | Water overflow from tank. |
Air leakage arrested | Deburring Machine | Air leakage. |
Pump dismantled from machine and kept in maintenance office. | Studer | Coolant leakage from pump. |
Sensor cleaned properly. | Studer | Door maintenance alarm. |
Motor replaced with new | Test Rig H1 | Drain motor running continuously. |
Multiple time restarted found ok checked in manually coolant on ok. | Kapp Wheel | Coolant of alarm. |
sensor replaced. | Assembly stations of CH02 | Job present signal missing |
Checked found neutral problem cable connected properly found ok. | PDI Assembly & PDI Packing Line 2 | Conveyer not working |
Restarted multiple time. | PDI Assembly & PDI Packing CH01 Line 1 | sensor not working |
Stud replace d1 | Test Rig D1 | Stud broken |
Tankline filter cleaning d1. | Test Rig G1 | Pressure high problem. |
filter cleaning d1. | Test Rig F2 | Imbalance QP. |
Found cobot clamping problem. So manually recovered. | Cleantech | Cobot stuck |
Found scanner not working so restarted and disconnected scanner cable and reconnected. | PDI Assembly & PDI Packing CH01 Line 1 | Scanner not working. |
Found do not lock properly so make machine reset. And machine shutdown d1 | Test Rig H2 | Door problem |
Found sensor faulty so changed sensor. | Studer Favorit | Job present sensor faulty |
Found Guage not reached position alarm came many times. Problem not solved Machine pending | Studer Favorit | Slide gauge not working. |
Found machine stopped during cycle time. So make machine reset. | ELB Wheel | NC stop during cycle time |
Found production hood alarm came so sensor cleaning d1. | Stahli S/F Grinding Machine 1 | Production hood alarm came. |
Found hydraulic oil level low so filled oil 9 litre. | ELB Wheel | Hydraulic oil level low. |
Nozzle cleaning d1. | ELB Wheel | Coolant flow problem |
check and reconnected the connector, | Store Punching Machine 1 | PC not turned on |
filter cleaning d1 | Test Rig H2 | Pressure to tank line filter choked |
check and alignment d1 locking element cleaned properly | Test Rig G2 | Door lock issue |
So checked and tightened properly | Test Rig D | Drain motor spline shaft lose |
Removed properly | Assembly station 2 | Need to remove fixture |
Adjusted accordingly | Bolt torquing (Assembly Station) | Need to adjust pin bolt present sensor. |
Reset plc | Assembly station 3 | Plc disconnect |
null | Studer Favorit | Fume extractor not working. Rcps |
Checked and adjusted flow | BVLINE PVG Test Stand | Right side door not open |
Checked and restarted machine | Cleantech | Conveyer Motor Trip |
Adjusted accordingly | Test Rig F1 | Need to adjust bolt torque tapping gun |
Adjusted torque, accordingly. | Test Rig E2 | Needs to adjust lapping gun torque |
Adjusted torque, accordingly. | Test Rig G2 | Needs to adjust lapping gun torque |
sensor setting d1, but problem repeated sensor replaced. | Studer 1 (450) | Conveyor job present sensor problem. |
Found coolant level low. Cleaned tank dirty tank not transfer coolant. clean tank filter block clean filter | ELB Wheel | Coolant flow problem |
Workpending | ELB Rim | Linear motor work |
Return line filter cleaned | Test Rig D1 | Pt high alarm |
Tool replaced, but problem stil exixts. So old tool fitted and removed extra support material form fixture. | PDI Assembly & PDI Packing CH01 Line 1 | Tool stuck in job |
Checked all connections found 1 wire loose so retightened but problems still same then checked door operation formed doors servicing bracket loose so bracket retired | Kapp Wheel | Coolant flow alarm |
Flow control interchanged and flow adjusted | Nissin | Pallet forward error. |