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Tightened all fittings and restarted machine
Jerk Testing
Pressure not developed
Properly clean the filter, then refitting d1
Test Rig F2
filter jammed
Manually increased the temperature
Test Rig D1
Temperature low problem
Sensor adjusted
PDI Assembly & PDI Packing CH01 Line 1
Job present sensor not working
Remove the palate manually
ELB Wheel
Pallet stuck.
Seal removed and so replace seal
Test Rig F1
Clamping issue
Checked 21.42 valve not operated. then relay interchanged But VSPP model job master input torque with server cycle torque not achieved. Other job tests, ok, set up changed 2 time
Test Rig E2
PT line pressure hig 60 bar
Checked servo drive not on at 3:00 AM. Drive on,
Test Rig D
Hydraulic not on QP problem
Cheeked and machine software restarted. Then model selected
Assembly station 3
Pin Bolt absent alarm
Sensor teaching d1
Stahli S/F Grinding Machine 1
Protection hood alarm
Panel relay interchanged
Test Rig G2
Neutral cycle qp problem
Checked 6.60 filter choked. Clean the filter
Test Rig F2
Pressure relief Q P not developed
Level sensor cleaning d1
Durr Ultrasonic
Work tank not empty alarm
Leakage to be arrested, but FRL housing side leakage found housing need to be checked
Studer Favorit
FRL unit air leakage
Pressure set
Piston Coining
Low pressure model problem
Fixer changed
Jerk Testing
Fixed to be changed
Clutch assembly and Spocket Bolts retightend
Test Rig E1 & E2
Neutral problem
Adjusted air pressure
Assembly stations of CH02
Pressure relief gun RPM slow.
Found plc error so reset
Assembly stations of CH03
Ball coining not start
Manually recovered
Nissin
Pellet stuck at Conveyer in machine
Found holding key missing so new key fitted
Assembly stations of CH06
Bolt tool not
Observe only number three fixture job not picked by cobot
Kadia 40
Job not picked from machine by cobot
Drain water from oil separator
Durr Ultrasonic
Oil separator overflow alarm
Found this aligned drain pipe so properly alignment d1 with magnetic separator
Studer
Water leakage on shop floor
So checked and found clutch assembly internal bolt loose, so tightened properly
Test Rig H1 & H2
Neutral test not OK.
So checked and found water line inlet filter is choked, so removed filter and cleaning d1 properly fitted
Test Rig D1 & D2
Temperature high
Fixed changed
Test Rig F2
Fixed to be change
PLC Communication Cable reconnection d1
Assembly station 2
P L C error
Checked and found load break and stuck in chamber properly connected found OK
Durr Ultrasonic
Basket stuck
check and found PLC ok, then restarted pc. Found working OK
BVLINE ECO 80 Test Stand
Emergency auto cycle, not working
Relay interchanged found working O K
Assembly stations of CH02
Gun not working
Removed manually from machine found ok.
Cleantech
Job stuck
Sensor adjusted
Centre Lapping
Job present sensor not on.
Found plc error, so error reset
Assembly stations of CH03
Dust seal sensor not on
Found noise in motor, but not work on machine due. This work will be d1 on plan work
Kadia 40
Abnormal noise on brush station
Found alignment problems so alignment d1
Cleantech
Onload side door not open
Turn on PC and handover to production
Assembly stations of CH06
PC not on
Found their job presents sensor not on so adjusted the sensor
Piston Coining
Cycle not start
Compressor LP and HP reset
Studer
Temperature problem
Removed job change logged &
Cleantech
Job stuck lock is not found
Transducer and valve placed at original position
Test Rig E2
Tranducer value at position
Removed scanner and connected them again
Test Rig H2
Scanner not operating
Fitted portable chiller unit and connected them( 17-23 Temperature present)
Studer
Chiller temperature is low
Found that ball stuck so removed
Assembly stations of CH03
Ball feeder not operate
Changed filter paper
Studer
filter paper is removed
Manually base positioning d1
Durr Ultrasonic
Base position problem came
Checked and QT value flow metre connector removed and reconnected.
Test Rig C
Qt value not so.
Checked minimise hose and cleaned with air.
Test Rig G2
Tankline pressure low.
Cycle test torque not ok manually adjusted.
Test Rig E2
VSSP model input torque with servo
Changed setup
Test Rig E1
Setup change
Return line filter cleaning d1 and refitting d1
Test Rig G1
Tank pressure high alarm
Coil connector removed and refitted then started valve and temperature ok.
Test Rig D
Temperature problem
cleaning d1 of filter
Test Rig G2
Return line filter choke
Adjusted the tool height then ok.
Dust Seal
Dust seal not press properly.
Changed setup
Test Rig E2
Setup change
New filter paper fitted d1.
Studer
Filter over
So checked & found Level 13 ok, but sensor wrong communicated. So remove these sensor, new sensor fitted d1.
Durr Ultrasonic
Oil skimmer tank fill minimum level alarm came
So checked and found clutch assembly removed all bolts and tightened & refitted
Test Rig E2
Neutral test not ok.
Panel underside code supply not on so checked 1 MCB tripped, so removed trip then machine restarted.
Test Rig F2
PLC Communication error
So big brush changing d1.
Deburring Machine
Brush changing work
Counter reset d1.
Nissin
Brush counter 13 over
Checked & found no alarm came, so make machine reset
ELB Wheel
M/c stopped in auto cycle
Found movomatic gauge alarm, so gauge connections open and Cleaned properly
Studer Favorit
Guage problem
Checked and found motor not started when given command so found capacitor not working. So change the capacitor
Test Rig F1
Drain motor problem.
Checked and found filtered jam so filter cleaning d1.
Test Rig D1
Tank pressure problem
Checked and found belt broken. So replaced with new belt
Stahli S/F Grinding Machine 1
Belt broken
Checked found door not open to Bolt stuck so manually open properly fitted Bolt again.
EMAG Rim
Front door problem.
Setup changed
Test Rig F1
Setup change
Dust seal tool loose so not working properly. Tighten the tool. Then trial taken OK
Assembly stations of CH06
Dust seal tool problem.
Set up boost change. New Bush fitting work d1
BVLINE ECO 80 Test Stand
Oil leakage from setup.
Oil top up d1, now lubrication oil level ok.
EMAG Rim
Lubrication oil level low
Table height, setting properly levelling ok.
PDI Assembly & PDI Packing CH01 Line 1
New PDI line inspecting table height problem.
Replace the job, then setting fixture properly
Assembly stations of CH03
Bolt torque fixture problem job stuck
filter changed tank number 1 new filter fitting d1.
Durr Ultrasonic
filter problem tank 1.
Setup changed
Test Rig E1
Setup change
Fitted MS bolt and nut.
Test Rig G2
Locking Bolt is not present
Adjusted pressure
Piston Coining
Pressure low problem.
Adjusted distance manually.
EMAG Rim
Clamping distance not proper.
Clean filter.
Knoll Coolant System
Filter clogged
Setup changed
Jerk Testing
Setup change
Brush changed ok.
Deburring Machine
Brush change
Return line filter cleaning d1.
Test Rig F1
Line filter blocked.
So checked and found mist collector filter cleaning d1.
EMAG Wheel
Job loading side fume came.
filter cleaning d1
ELB Rim
Filter choked
So tension adjusted
Deburring Machine
Belt tension loose
Spray pump counter is stack up. so Reset.
Cleantech
Spray pump counter stuck.
Table properly levelling d1.
PDI Assembly & PDI Packing CH01 Line 1
Table levelling work.
Tpm programme changing d1.
Assembly stations of CH03
Shock valve direction not okay.
Sensor sitting d1
Assembly stations of CH03
Spool set assembly clamping problem.
Set up change d1.
Test Rig E1
Set up change work.
So cheked & found flowmeter setting properly d1.
ELB Rim
Coolant level low, but pressure not to stop.
Cheeked and found sensor properly setting d1.
Piston Coining
Station 2 signal missing
check tankline filter cleaning d1
Test Rig F2
Pressure high problem.
check machine position ok.
ELB Rim
Coolant flow problem.
Sensors set properly
Studer Favorit
gauge side problem
check found slug cleaning d1
Studer Favorit
Magnetic separator overflow.
check cylinder sensor setting d1.
Nissin
Job clamping problem.
Plc error manually reset d1.
Assembly stations of CH04
Plc error.
So sensor adjusted properly
EMAG Rim
Job present sensor malfunctioning.
Checked found spindle bearing jam and drive overloaded. So Alarm reset.
ELB Rim
HSB drive fault.