output
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Tightened all fittings and restarted machine | Jerk Testing | Pressure not developed |
Properly clean the filter, then refitting d1 | Test Rig F2 | filter jammed |
Manually increased the temperature | Test Rig D1 | Temperature low problem |
Sensor adjusted | PDI Assembly & PDI Packing CH01 Line 1 | Job present sensor not working |
Remove the palate manually | ELB Wheel | Pallet stuck. |
Seal removed and so replace seal | Test Rig F1 | Clamping issue |
Checked 21.42 valve not operated. then relay interchanged But VSPP model job master input torque with server cycle torque not achieved. Other job tests, ok, set up changed 2 time | Test Rig E2 | PT line pressure hig 60 bar |
Checked servo drive not on at 3:00 AM. Drive on, | Test Rig D | Hydraulic not on QP problem |
Cheeked and machine software restarted. Then model selected | Assembly station 3 | Pin Bolt absent alarm |
Sensor teaching d1 | Stahli S/F Grinding Machine 1 | Protection hood alarm |
Panel relay interchanged | Test Rig G2 | Neutral cycle qp problem |
Checked 6.60 filter choked. Clean the filter | Test Rig F2 | Pressure relief Q P not developed |
Level sensor cleaning d1 | Durr Ultrasonic | Work tank not empty alarm |
Leakage to be arrested, but FRL housing side leakage found housing need to be checked | Studer Favorit | FRL unit air leakage |
Pressure set | Piston Coining | Low pressure model problem |
Fixer changed | Jerk Testing | Fixed to be changed |
Clutch assembly and Spocket Bolts retightend | Test Rig E1 & E2 | Neutral problem |
Adjusted air pressure | Assembly stations of CH02 | Pressure relief gun RPM slow. |
Found plc error so reset | Assembly stations of CH03 | Ball coining not start |
Manually recovered | Nissin | Pellet stuck at Conveyer in machine |
Found holding key missing so new key fitted | Assembly stations of CH06 | Bolt tool not |
Observe only number three fixture job not picked by cobot | Kadia 40 | Job not picked from machine by cobot |
Drain water from oil separator | Durr Ultrasonic | Oil separator overflow alarm |
Found this aligned drain pipe so properly alignment d1 with magnetic separator | Studer | Water leakage on shop floor |
So checked and found clutch assembly internal bolt loose, so tightened properly | Test Rig H1 & H2 | Neutral test not OK. |
So checked and found water line inlet filter is choked, so removed filter and cleaning d1 properly fitted | Test Rig D1 & D2 | Temperature high |
Fixed changed | Test Rig F2 | Fixed to be change |
PLC Communication Cable reconnection d1 | Assembly station 2 | P L C error |
Checked and found load break and stuck in chamber properly connected found OK | Durr Ultrasonic | Basket stuck |
check and found PLC ok, then restarted pc. Found working OK | BVLINE ECO 80 Test Stand | Emergency auto cycle, not working |
Relay interchanged found working O K | Assembly stations of CH02 | Gun not working |
Removed manually from machine found ok. | Cleantech | Job stuck |
Sensor adjusted | Centre Lapping | Job present sensor not on. |
Found plc error, so error reset | Assembly stations of CH03 | Dust seal sensor not on |
Found noise in motor, but not work on machine due. This work will be d1 on plan work | Kadia 40 | Abnormal noise on brush station |
Found alignment problems so alignment d1 | Cleantech | Onload side door not open |
Turn on PC and handover to production | Assembly stations of CH06 | PC not on |
Found their job presents sensor not on so adjusted the sensor | Piston Coining | Cycle not start |
Compressor LP and HP reset | Studer | Temperature problem |
Removed job change logged & | Cleantech | Job stuck lock is not found |
Transducer and valve placed at original position | Test Rig E2 | Tranducer value at position |
Removed scanner and connected them again | Test Rig H2 | Scanner not operating |
Fitted portable chiller unit and connected them( 17-23 Temperature present) | Studer | Chiller temperature is low |
Found that ball stuck so removed | Assembly stations of CH03 | Ball feeder not operate |
Changed filter paper | Studer | filter paper is removed |
Manually base positioning d1 | Durr Ultrasonic | Base position problem came |
Checked and QT value flow metre connector removed and reconnected. | Test Rig C | Qt value not so. |
Checked minimise hose and cleaned with air. | Test Rig G2 | Tankline pressure low. |
Cycle test torque not ok manually adjusted. | Test Rig E2 | VSSP model input torque with servo |
Changed setup | Test Rig E1 | Setup change |
Return line filter cleaning d1 and refitting d1 | Test Rig G1 | Tank pressure high alarm |
Coil connector removed and refitted then started valve and temperature ok. | Test Rig D | Temperature problem |
cleaning d1 of filter | Test Rig G2 | Return line filter choke |
Adjusted the tool height then ok. | Dust Seal | Dust seal not press properly. |
Changed setup | Test Rig E2 | Setup change |
New filter paper fitted d1. | Studer | Filter over |
So checked & found Level 13 ok, but sensor wrong communicated. So remove these sensor, new sensor fitted d1. | Durr Ultrasonic | Oil skimmer tank fill minimum level alarm came |
So checked and found clutch assembly removed all bolts and tightened & refitted | Test Rig E2 | Neutral test not ok. |
Panel underside code supply not on so checked 1 MCB tripped, so removed trip then machine restarted. | Test Rig F2 | PLC Communication error |
So big brush changing d1. | Deburring Machine | Brush changing work |
Counter reset d1. | Nissin | Brush counter 13 over |
Checked & found no alarm came, so make machine reset | ELB Wheel | M/c stopped in auto cycle |
Found movomatic gauge alarm, so gauge connections open and Cleaned properly | Studer Favorit | Guage problem |
Checked and found motor not started when given command so found capacitor not working. So change the capacitor | Test Rig F1 | Drain motor problem. |
Checked and found filtered jam so filter cleaning d1. | Test Rig D1 | Tank pressure problem |
Checked and found belt broken. So replaced with new belt | Stahli S/F Grinding Machine 1 | Belt broken |
Checked found door not open to Bolt stuck so manually open properly fitted Bolt again. | EMAG Rim | Front door problem. |
Setup changed | Test Rig F1 | Setup change |
Dust seal tool loose so not working properly. Tighten the tool. Then trial taken OK | Assembly stations of CH06 | Dust seal tool problem. |
Set up boost change. New Bush fitting work d1 | BVLINE ECO 80 Test Stand | Oil leakage from setup. |
Oil top up d1, now lubrication oil level ok. | EMAG Rim | Lubrication oil level low |
Table height, setting properly levelling ok. | PDI Assembly & PDI Packing CH01 Line 1 | New PDI line inspecting table height problem. |
Replace the job, then setting fixture properly | Assembly stations of CH03 | Bolt torque fixture problem job stuck |
filter changed tank number 1 new filter fitting d1. | Durr Ultrasonic | filter problem tank 1. |
Setup changed | Test Rig E1 | Setup change |
Fitted MS bolt and nut. | Test Rig G2 | Locking Bolt is not present |
Adjusted pressure | Piston Coining | Pressure low problem. |
Adjusted distance manually. | EMAG Rim | Clamping distance not proper. |
Clean filter. | Knoll Coolant System | Filter clogged |
Setup changed | Jerk Testing | Setup change |
Brush changed ok. | Deburring Machine | Brush change |
Return line filter cleaning d1. | Test Rig F1 | Line filter blocked. |
So checked and found mist collector filter cleaning d1. | EMAG Wheel | Job loading side fume came. |
filter cleaning d1 | ELB Rim | Filter choked |
So tension adjusted | Deburring Machine | Belt tension loose |
Spray pump counter is stack up. so Reset. | Cleantech | Spray pump counter stuck. |
Table properly levelling d1. | PDI Assembly & PDI Packing CH01 Line 1 | Table levelling work. |
Tpm programme changing d1. | Assembly stations of CH03 | Shock valve direction not okay. |
Sensor sitting d1 | Assembly stations of CH03 | Spool set assembly clamping problem. |
Set up change d1. | Test Rig E1 | Set up change work. |
So cheked & found flowmeter setting properly d1. | ELB Rim | Coolant level low, but pressure not to stop. |
Cheeked and found sensor properly setting d1. | Piston Coining | Station 2 signal missing |
check tankline filter cleaning d1 | Test Rig F2 | Pressure high problem. |
check machine position ok. | ELB Rim | Coolant flow problem. |
Sensors set properly | Studer Favorit | gauge side problem |
check found slug cleaning d1 | Studer Favorit | Magnetic separator overflow. |
check cylinder sensor setting d1. | Nissin | Job clamping problem. |
Plc error manually reset d1. | Assembly stations of CH04 | Plc error. |
So sensor adjusted properly | EMAG Rim | Job present sensor malfunctioning. |
Checked found spindle bearing jam and drive overloaded. So Alarm reset. | ELB Rim | HSB drive fault. |