output
stringlengths
5
373
input
stringclasses
110 values
instruction
stringlengths
6
132
Somehow fixed the leg & alignment d1 of the conveyor, problem solved. But need to change the legs if damaged again.
PDI Assembly & PDI Packing CH01 Line 1
Conveyor table leg broken
Setup changed.
BVLINE PVM Test Stand
Setup change
Dismentling of spindle doen, new spindle fitting pending.
EMAG Rim
Spindle change
Alignment d1 properly
Kadia 40
Alignment prpoblem
Released the extracted then cycle started.
Cleantech
Spray pump trip problem
Motor production contractor.
Stahli S/F Grinding Machine 1
Wheel operating reverse direction
Checked 6.5 filter cleaning d1, but problem not solved. So replaced filter
Test Rig F2
Pressure relief cycle qp problem.
So sensor properly setting d1
Studer
Guage sensor disturbed
Checked cylinder sensor disturbed so sensor properly set
Deburring Machine
Cycle not start, deburing cylinder not reduce
Chevrolet emergency balls not coming. So ball feeder fixture alignment d1.
Assembly stations of CH06
Emergency ball feeder problem.
null
Assembly stations of CH03
Bolt torque machine job loading side fixture topside Burr.
Checked and found cobot Reed switch wire broke from gripper, so connected properly.
Cobot of Studer
Cobot not working.
Chikkadan found sensor position disturbed. So adjusted properly.
Micromatic Grinding
Job present sensor problem.
Checked and found wire lose so tightened properly.
Stahli S/F Grinding Machine 1
Wheel auto off
Checked & found coolant not coming during dressing time so found coolant on off automation seal damage so interchanged with 450 automation.
Studer 3 (452)
Coolant problem.
Found that paper is stack, so removed and trial taken from OK
Test Rig F1
Oil not drain.
Found that job is stuck so manually recovered
Cleantech
X44 manifold not operating
Top up d1 of lubrication oil
Cleantech
Lubrication oil low.
Changed bag filter.
Durr Ultrasonic
Tank 1 exceed alarm came
Sensor cleaned
Stahli S/F Grinding Machine 1
Protection hood not down
Cable properly jointed , But problem came after cycle. Need to check further
PDI Assembly & PDI Packing CH01 Line 1
Y axis alarm came
Arrested air leakage,
PV Assembly & Leak Testing
Air leakage
Manually recovered and checked all alignment and base positioning d1
Durr Ultrasonic
Ball position not down
Spindle changed
EMAG Rim
Spindle changed
6.05 filter cleaned
Test Rig F1
QP problem
Door rail alignment d1 and sensor cable properly fitted.
Test Rig E2
Door problem
Arrested oil leakage and valve checked need to check further
PV Assembly & Leak Testing
Pilot valve problem ( Master not ok )
Manually based positioning d1, but problem came. Need to check further
Durr Ultrasonic
Base position problem.
6.5 filter cleaning d1
Test Rig F2
QP pressure drop
Checked and found clamping sensor not working. So
Test Rig C
Camping problem
Checked and sensor cleaning d1
Stahli S/F Grinding Machine 1
Protection hood alarm
Checked and found job present sensor not working. So adjusted properly for temporarily
Studer
Job Present sensor problem.
Checked & found machine not in home position so taking machine in home position
Cleantech
M/C auto cycle off
Checked and found seal damaged so new seal fitted properly.
Test Rig A
Seal problem.
Checked & found machine auto hang so make machine shutdown and restarted
Studer 1 (450)
Machine auto hang.
Checked and found temperature down so Manually recovered.
Test Rig D1
Temparature problem
Checked & found dust seal sensor problem so adjusted properly.
Assembly stations of CH04
Dust seal problem
Checked and found scanner not working. So scanner cleaning properly.
Assembly stations of CH03
Scanner not working.
Manually recovered.
Cleantech
Cycle not to start.
Checked and found hydraulic oil leakage. Oil level and then PU connector retightend & oil top up d1, but problem not solved. Then checked all. Found on valve properly not closed due to solenoid valve problem. So solenoid valve replaced and trial taken. OK, Work delay due to temperature not achieved.
PV Assembly & Leak Testing
Leak test not okay
Checked found ball not coming ball feeder alignment d1
Assembly stations of CH06
Ball feeder problem
Restarted the machine then manually control the machine, trial taken. Then auto cycle started running. OK,
Studer 2 (451)
Cycle not start.
Checking then found that the basket not setting properly. So after all, sensors checking d1, then found that inside machine, the basket holding conveyor Bolt was broken, so properly fitting new Bolt. Then tried again. Found ok. Machine handover to production team
Durr Ultrasonic
Basket stuck.
So filled the oil separator then manually positioning d1 then auto cycle started
Durr Ultrasonic
Oil separator minimum alarm coming.
After checking, found that cylinder not working properly. So new cylinder logic applying
Kapp Wheel
Door not operate
After checking found the label sensor problem, not working properly. So after cleaning the sensor, problem solved.
Nissin
Coolant tank unit contractor fluctuate continuously
So checked & machine alignment d1.
Assembly stations of CH02
Emg ball not coming
Changed setup accordingly
Test Rig E1
Need to changed setup
Air leakage arrested
Cleantech
Air leakage
Sensor set properly
Test Rig C
Clamping sensor problem
So checked clutch assembly all bolt tightened and fitted properly and line filter cleaned and interchanged flow metre with new 1, but still same problem. handover to C shift
Test Rig E2
Neutral & inbalance QP problem
So manually base positioning operated then base home position ok.
Durr Ultrasonic
Base position disturbed
Power restarted
Emag China
Power supply fault of drive.
Checked cooling unit push button through connector on after some time MPCB trip. Checked compressor resistance found ok power cable removed then MPCB ok. Need to check with Megear to compressor.
EMAG Rim & Wheel
Cooling unit fault
Checkdant found forward sensor faulty
Studer
Gauge unit fault
Found job present sensor mounting not properly d1, mounting plate fixed.
Studer
Job clamp declamp problem.
Setup changed.
Test Rig E2
Setup change
Found MPCB triped, so MPCB on,
Test Rig F1
Hydraulic motor trip
Adjusted sensor
Studer
Job not clamping
Setup changed
Test Rig E1 & E2
Setup change work
Found disc is loose, so tightened them
Assembly stations of CH02
Ball not coming
adjusted sensor
Bolt torquing (Assembly Station)
Pin bolt absent alarm
Sensor cleaning d1,
Assembly stations of CH06
Scanner problem
PC restarted
Assembly stations of CH04
PC problem
Manually set
Piston Coining
Pressure not develpoed
Sensors adjusted
Studer
Job not clamp
PLC reset d1
Assembly stations of CH06
System Hang
PM D1
Durr Ultrasonic
PM Activity
Power restarted
EMAG Wheel
A axis fault
Found coolant oil level low due to filtration not working properly. SO told Sachin for cleaning.
ELB Wheel
Comp1nt burn problem.
Hieght adjusted properly
Test Rig E1 & E2
Drain motor and torque gun height to be set.
Tail stuck oil top-up d1
Studer
Tail stuck oil level, low
Power restarted.
EMAG Wheel
Power supply of drive fault
Checked & found circulation motor & fan found working ok. Compressor found body shock
ELB Rim
Compressor tripped
Checked & found circulation motor & fan found working ok. Compressor found body shock
EMAG Rim
Compressor tripped
Bypassed switch connections tightened properly,
Stahli S/F Grinding Machine 1
Spindle stoped during
PM Completed as per checksheet.
BVLINE Test Stand A(Dual stage)
PM Plans
PM Completed as per checksheet.
EMAG Rim
PM Plans
Roller bearing not working bearing damage so replaced that bearing new 1 fitting d1 .
Studer Favorit
Magnetic separator
Changed the filters, then cleaning the fume extractor d1.
Cleantech
Fume extractor problem.
Checking the leakage, then cleaning the machine properly. Machine under observation
Durr Ultrasonic
Leakage problem
Oil leakage from the hydraulic pipe connector. So open the fitting then Using Teflon tape re tighten the pipe again .
EMAG Rim
Oil leakage.
So replace the gun from CH5. The CH5 gun fitting d1 at CH3
Bolt torquing (Assembly Station)
Gun Not working.
After opening the magnetic separator, found that the separator working ok, but oil is producing foam. Found oil leakage from side. So this problem is under process
Nissin
Magnetic separator problem.
So filtered cleaning d1.
Store Laser Punching Machine 1
Blower filter problem.
PM Completed as per checksheet.
Assembly stations of CH01
PM Activity
PM Completed as per checksheet.
ELB Oil Filtration Unit
PM Activity
New sensor cable property routing d1
Stahli S/F Grinding Machine 1
Protection hood sensor problem.
PM Completed as per checksheet.
ELB Oil Filtration Unit
PM Activity
Found alarm on controller so reset d1 tehn started cycle.
Centre Lapping
Cycle not start
Found safty cutain issue, so align safty cutain
Deburring Machine
Cycle not start
Torque Gun height adjusted and drain motor also.
Test Rig E1 & E2
Drain motor and Torque gun height problem.
Trailed some cycle found all cycle okay.
Test Rig F2
In balance, QP cycle not ok
Found clean tank water level low so water top up d1.
Cleantech
Cycle not start
Found valve closed so valve opened
BVLINE PVG Test Stand
Air pressure low
Found main air pressure low so New airline provided
BVLINE ECO 80 Test Stand
Cycle not okay due to pressure low
After checking valve changing d1, then trial taken. But after that, foam coming again. Then Bush changing d1.
Test Rig F2
QP problem
Found valve o-ring damage so o-ring replaced.
Studer 1 (450)
Coolant oil leakage
Checked and found Convoyer jammed so after moving forward and reverse of Motor jam solved,
BVLINE Assembly Station(Single Stage)
Conveyor not start.
Found push button continuously on so after removing the rubber, the problem solved
KLEIN 3
Cycle not start