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At 1341, the airplane was issued a low altitude alert and the pilot reported that he was "having a hard time holding altitude." At that time, the airplane was about 10 miles north of HSV, at an altitude of about 1,700 feet.
At 1343, the airplane was cleared to land on runway 18R, a 12,600-foot-long, asphalt runway.
The airplane's last radar target was recorded at 1345, at an altitude of 800 feet, about 3 miles north of the airport.
Witnesses observed the airplane flying toward the airport at a low altitude, with the right engine not operating.
One witness stated that he also observed the right engine "cover or cowling propped up." Another witness observed the airplane impact tree tops and then "nose dive straight in the ground." The airplane was engulfed in flames upon impact.
PERSONNEL INFORMATION The pilot, age 52, held a private pilot certificate, with ratings for airplane single-engine land, airplane multiengine land, and instrument airplane.
Pilot logbooks found at the accident site were compromised due to fire, water and impact damage.
The pilot reported 1,600 hours of total flight experience, which included 52 hours in the past 6 months on his most recent application for an FAA third-class medical certificate, which was issued on November 4, 2009.
He reported 1,350 hours of total flight experience, which included 60 hours in the past 6 months, on an FAA third-class medical certificate application dated November 21, 2006.
AIRCRAFT INFORMATION According to FAA records, the pilot purchased the airplane on March 26, 1998.
The six seat-seat, low-wing, retractable-gear airplane, serial number P-591, was manufactured in 1982.
It was powered by two Lycoming TIO-541-E1C4, 380-horsepower engines that were each equipped with a Hartzell constant-speed, full-feathering, three-bladed propeller.
Review of maintenance records revealed that the airplane had undergone an annual inspection on May 20, 2009, at a total airframe time of 3,383 hours.
At the time of the accident, the airplane had been operated for about 50 hours since the annual inspection.
The right engine had been operated for about 1,425 hours since it was overhauled on October 10, 1995.
On April 11, 2003, at an engine total time of 970.5 hours, the No.
2 cylinder was removed for the replacement of "all 4 small case studs" and the "large forward top...and lower stud." The left engine had been operated about 270 hours since it was installed on March 1, 2006, after being overhauled.
METEOROLOGICAL INFORMATION A weather observation taken at HSV (elevation 629 feet), about the time of the accident reported, calm winds; visibility 10 statute miles; few clouds at 25,000 feet, temperature 13 degrees Celsius (C), dew point 7 degrees C; altimeter 30.05 inches of mercury.
WRECKAGE AND IMPACT INFORMATION The airplane struck the tops of about 70-foot tall trees and impacted the ground within a housing development, approximately 3 miles north-northeast of HSV.
The initial ground scar was located about 30 feet northeast of the main wreckage.
Several freshly cut tree branches, which exhibited 45-degree cuts were observed at the accident site.
The airplane came to rest upright, on a heading of about 165-degrees magnetic.
All major portions of the airframe were accounted for at the accident site.
The majority of the airframe, which included the left wing, cabin, and the airframe structure aft of the rear pressure bulkhead, was consumed by fire.
The remaining portions of the airframe and both engines sustained significant fire damage.
The right engine throttle, mixture, and propeller controls in the cockpit were observed in an aft position, and the right fuel selector handle was in the "OFF" position.
The left engine throttle, mixture, and propeller controls were observed in a forward position, and the left fuel selector handle was about 10 degrees left of the "ON" position.
Measurement of the left and right flap actuators corresponded with a 0-degree flap position.
The landing gear actuators' position at the landing gear retract gearbox was consistent with the landing gear in the retracted position.
The right engine remained partially attached to the airframe.
The right engine propeller assembly was separated and partially buried in the ground, near the initial ground scar.
All three propeller blades were in a low pitch position and did not display evidence consistent with rotation.
A 5 1/2 by 6 inch hole was observed in the top right portion of the crankcase.
In addition, the crankcase was circumferentially cracked through the No.'s 1 and 3 cylinders.
The No.
2 cylinder assembly was separated from the engine and located 40 feet beyond the main wreckage.
Evidence of chaffing was observed between the No.'s 2 and 4 cylinder cooling fins.
The No.
2 connecting rod and connecting rod cap were also separated and located in the debris path.
The No.
2 piston and piston pin were not recovered.
The engine could not be rotated.
All spark plugs were removed and their electrodes were intact.
A borescope examination of cylinder No.'s 1, and 3 through 6, did not reveal any anomalies.
Both magnetos remained attached.
The right magneto was destroyed by fire.
The left magneto was removed and sparked on all towers when rotated by hand.
Metallic debris was observed in the oil sump; however, the oil filter was absent of visible metallic debris.
The right engine was retained for further examination.
The left engine was separated and located 28 feet prior to the main wreckage.
The propeller remained attached.
All three propeller blades displayed leading edge gouges and chordwise scratches consistent with rotation.
Both magnetos remained attached.
The right magneto was fire damaged and did not spark when rotated by hand.
The left magneto sparked on all towers when rotated.
The crankshaft was rotated via the crankshaft flange.
Thumb compression was attained and valve train continuity was observed on all cylinders.
All spark plugs were removed and their electrodes were intact.
Fuel was observed in the fuel inlet.
The fuel inlet and oil suction screens were absent of debris.
A borescope examination of all cylinders did not reveal any anomalies that would have precluded normal engine operation.
Additional examination of both propellers was conducted by a representative of Hartzell Propeller Inc., under the supervision of an NTSB investigator.
All propeller damage was consistent with impact damage and there were no discrepancies that would have precluded normal engine operation.
The left propeller was confirmed to be at a low pitch and rotating at the time of the impact; however, an estimation of power output could not be determined.
The right propeller was at a low pitch and did not have evidence of rotation.
It could not be determined if the propeller had been feathered prior to impact.
The right engine was examined at Lycoming Engines, Williamsport, Pennsylvania, under the supervision of an NTSB Investigator.
During the examination, it was noted that the rear top 3/8-inch and the front top 1/2-inch cylinder hold down studs for the No.
2 cylinder exceeded the manufacturers specified length from the case deck by .085 and .111 inches; respectively.
In addition, grease was found on all thru studs, contrary to Lycoming installation procures.
The teardown did not reveal any failures pertaining to cylinder assemblies other than the No.
2 cylinder.
The No.
2 connecting rod, No.
2 cylinder, two through bolts, and portions of the engine crankcase where the No.
2 cylinder would have been mounted were retained and forwarded to the Safety Board's Materials Laboratory, Washington, DC, for further examination.
MEDICAL AND PATHOLOGICAL INFORMATION Autopsies were performed on the pilot and passenger by the Alabama Department of Forensic Sciences, Huntsville, Alabama, on January 19th and 20th, 2010; respectively.
Toxicological testing was performed on the pilot by the FAA Bioaeronautical Science Research Laboratory, Oklahoma City, Oklahoma, with no anomalies noted.
TESTS AND RESEARCH According to the NTSB Metallurgist's Factual report, examination of the retained right engine components revealed in part, that the No.
2 cylinder had plastic deformation and tearing of the skirt at the base of the cylinder where it would have mated to the crankcase.
The damage was consistent with overstress and did not suggest any preexisting anomalies.
One of the through bolts had failed due to a fatigue fracture and the other failed due to an overstress fracture.
Additionally, one of the cylinder studs failed due to a fatigue fracture and a fatigue fracture was also observed on the right side of a portion of the crankcase, which remained attached to the cylinder.
The fracture was in a plane mostly perpendicular to the threaded bore of the cylinder stud.
In addition, the surface of the crankcase surrounding the bore for the through bolt was slightly depressed in the area that would have been covered by the No.
2 cylinder flange.
[For additional information please see the NTSB Metallurgical Factual Report located in the public docket.] ADDITIONAL INFORMATION Aircraft Performance The aircraft manufacturer calculated the airplane's climb performance based on an estimated gross weight of 6,400 pounds, with one propeller stopped (not feathered), with the atmospheric conditions present at the time of the accident.
The airplane's maximum rate of climb at an altitude of 6,000 feet and at the accident site elevation was determined to be 191, and 341 feet-per-minute; respectively.
The pilot of the helicopter air ambulance performed an approach and landing to a rooftop heliport in gusting wind conditions, during which he reduced collective pitch control friction to more readily apply collective control inputs.
After landing, he started the after-landing portion of the checklist and turned the throttle twist grip on the collective from FLIGHT to IDLE, believing that he had engaged the collective lock.
Shortly thereafter, the collective "popped up," and the helicopter became airborne.
He immediately grabbed the cyclic with his right hand, the collective with his left hand, and twisted the twist grip to FLIGHT.
The helicopter then landed hard, resulting in minor damage.
Review of onboard video revealed a sequence of events consistent with the pilot鈥檚 statement, and recorded data indicated that the collective rose up consistent with it not locked in the down position and resulted in the engine transitioning from IDLE to FLIGHT.
This confirmed the pilot鈥檚 observation that the collective rose uncommanded.
The helicopter was designed to be convertible from a dual-pilot configuration (for activities such as training), to single-pilot configuration (for activities such as air ambulance).
Two days before the incident, the helicopter had been converted to the single-pilot configuration by a mechanic.
This conversion required that the collective be balanced to avoid uncommanded movement; however, post-incident examination of the helicopter revealed that the collective would rise unassisted, indicating that the collective was improperly balanced after the helicopter was converted to the single-pilot configuration.
The National Transportation Safety Board determines the probable cause(s) of this incident to be: The pilot鈥檚 failure to lock the collective pitch control after landing, and the mechanic鈥檚 failure to properly balance the collective pitch control after converting the helicopter to a single-pilot configuration, which resulted in an uncommanded collective movement and subsequent hard landing.
HISTORY OF FLIGHT On January 28, 2018, about 1400 central standard time, an Airbus Helicopters EC 130 T2, N894GT, incurred minor damage when it was involved in an incident in Memphis, Tennessee.