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The lineman, while subsequently refueling another airplane, only looked at the accident airplane periodically, but did see the ATP walking around it with the two passengers following him, and also saw him in the position required to activate the fuel strainer lever in the interior, right side of the cabin.
The lineman later drove by the airplane and noticed a puddle, an estimated 1 foot in diameter, on the tarmac below the fuel strainer.
The lineman also stated that the airplane's right tire was low, but that the airplane started and departed before he could inform the ATP.
He further observed that the ATP was in the front left seat, and that the younger passenger was in the front right seat.
The lineman advised the FBO manager of the underinflated tire, who then watched the airplane during the run-up, and also the takeoff in case assistance was needed.
The manager noted that the engine run-up was much quicker than he was accustomed to seeing.
He then saw the airplane taxi onto runway 16, and heard an "abrupt" addition of power for takeoff.
The airplane subsequently lifted off in the vicinity of taxiway Bravo, with the engine sounding "normal, real strong." An audition of tower communications revealed that, at 1708, the pilot called for taxi.
The tower controller approved taxi to either runway 16 or 34, pilot's discretion, and the ATP chose runway 16.
At 1712, a pilot requested and was cleared for takeoff, and was advised to then turn right, on course.
At 1713, the airplane was cleared to contact Jackson Departure Control.
A combined FAA radar depiction with voice overlay first revealed the airplane when it was just south of the departure end of runway 16 at an altitude of 500 feet.
At 1713:50, while the airplane was passing through about 700 feet, a pilot contacted departure control.
The controller requested that the pilot "ident" and he provided the local altimeter setting.
The pilot did not respond.
At 1714:05, the airplane reached 1,000 feet, followed by a descent to 900 feet.
At 1714:15, a pilot stated "we got an engine problem, we're turning back toward Hawkins." The controller responded, "requiring any assistance, you can turn left or right direct Hawkins," and the pilot replied, "we're headed back, we'll try to make it." The controller then stated, "understand you're declaring an emergency," but there were no further transmissions from the airplane.
Radar indicated a right, descending turn, with the last contact at 500 feet.
The ATP, age 65, held an airline transport pilot certificate with airplane single engine land, airplane multiengine land, and rotorcraft-helicopter ratings.
He also had commercial privileges for airplane single engine sea, glider, and lighter-than-air balloon aircraft.
In addition, he held type ratings for four helicopter types and a Lear 45.
He was also a certificated flight instructor, ground instructor, and mechanic.
The pilot's latest FAA second class medical certificate was dated August 14, 2012.
According to the ATP's logbook, he had accumulated 17,775 total flight hours, with 2,664 hours in single engine land airplanes, 2,804 hours in multiengine land airplanes, and 9 hours in the 30 days prior to the accident.
On an insurance application for the accident airplane dated March 30, 2012, the ATP indicated 294 hours in make and model.
Logbook entries indicated that subsequent to that date, he had an additional 28 hours in make and model.
Logbook entries also indicated 142 hours in the accident airplane, with the last flight in that airplane prior to the accident flight occurring on September 3, 2012.
The airplane, manufactured in 1972, was powered by a Lycoming TIO-540-series engine.
The airplane's latest annual inspection occurred on March 2, 2012, at 4,385 total airframe hours, and 751 hours since engine overhaul.
Based on the ATP's logbook, the airplane flew an estimated 28 additional hours before the accident.
According to the owner, the airplane had been sitting in its hangar with the fuel tanks half full.
A fuel log and the FBO lineman indicated that just prior to the flight, the ATP requested that the main fuel tanks be topped off with fuel, which resulted in 28.4 gallons being pumped.
The HKS Tower observation, at 1715, included clear skies, wind from 010 degrees true at 3 knots, visibility 10 statute miles, temperature 11 degrees C, dew point -2 degrees C, altimeter setting 30.33 inches Hg.
The majority of the airplane came to rest upside down in a house located in a populated area about 185 degrees true, 0.8 nautical miles south of the departure end of runway 16, in the vicinity of 32 degrees, 18.93 minutes north latitude, 090 degrees, 13.28 minutes west longitude.
Tree damage indicated an approximately 60-degree descent, heading 310 degrees magnetic.
Except for the left wing, which was lying in the yard next door, the airplane was mostly consumed in a postcrash fire, inside the house.
All flight control surfaces were accounted for at the scene.
Fire damage precluded flight control continuity beyond cable separation points.
The airplane's instrument panel was completely destroyed; however, charred remnants from a hand-held GPS receiver were recovered and forwarded to the NTSB Recorders Laboratory for a data recovery attempt which was not successful.
Engine power control positions could not be determined, and the fuel tank selector position at the time of impact could also not be ascertained.
The fuel tank selector was examined at the NTSB Materials Laboratory; however, no witness marks or other identifying features were found to note what tank position the fuel selector was in.
The Lycoming IO-540-series engine was also charred, with all accessories exhibiting thermal damage.
The engine was removed from its upside-down position, and placed on a flatbed trailer for further examination.
The propeller, which had one blade tip burned off, did not exhibit torsional bending or leading edge damage.
Propeller rotation confirmed crankshaft continuity to the back of the engine as well as valve movement.
Top spark plugs were removed, and cylinder compression was confirmed; however, as compressions were tested, dirty water, consistent with fire suppression water mixed with engine fluids, was ejected from the spark plug holes.
When the fuel flow divider (spider) was opened, water (noted visually and by taste) was found in the lower part that was clear with the exception of a small amount of white particulate matter.
- Fuel System – From the Cherokee Six 300 flight manual, "Standard fuel capacity…is 84 gallons, all of which is useable except for approximately one pint in each of the four tanks.
The two main inboard tanks…hold 25 gallons each…the tip tanks hold 17 gallons each.
The fuel selector control is located below the center of the instrument panel on the sloping face of the control tunnel…When using less than the standard 84 gallon capacity of the tanks, fuel should be distributed equally between each side, filling the tip tanks first." The fuel system should be drained daily prior to first flight and after refueling to avoid the accumulation of water or sediment.
Each fuel tank is equipped with an individual quick drain located at the lower inboard rear corner of each tank.
The fuel strainer and a system quick drain valve are located in the fuselage at the lowest point of the fuel system.
It is important that the fuel system be drained in the following manner: 1.
Drain each tank through its individual quick drain located at the lower inboard rear corner of the tank, making sure that enough fuel has been drained to ensure that all water and sediment is removed.2.
Place a container under the fuel sump drain outlet, which is located under the fuselage.
3.
Drain the fuel strainer by pressing down on the lever located on the right-hand side of the cabin below the forward edge of the rear seat.
The fuel selector must be positioned in the following sequence: off position, left tip, left main, right main, and right tip while draining the strainer to ensure that the fuel lines between each tank outlet and each strainer are drained as well as the strainer.
When the fuel tanks are full, it will take approximately 11 seconds to drain all the fuel in one of the lines between a tip tank and the fuel selector, and approximately 6 seconds to drain all the fuel in one of the lines from a main tank to the fuel strainer.
When the tanks are less than full, it will take a few seconds longer.4.
Examine the contents of the container placed under the fuel sump drain outlet for water and sediment and dispose of the contents.
- Fuel Quality - According to the manager of the FBO, the fuel truck was sumped daily.
A fuel sample was taken from the truck after the accident by FBO personnel within 20 minutes of the accident, examined, and found to contain no water, debris or other anomalies.
It was not retained by authorities prior to NTSB visit to HKS, but remained with the FBO and was not subsequently tested.
According to the FBO fueling log, on the date of the accident, the airplane received 28.4 gallons of fuel from the FBO's fuel truck.
The log also indicated that five airplanes had been fueled before the accident airplane, receiving a total of 279.1 gallons from the fuel truck, and after the fuel sample was taken subsequent to the accident, one additional airplane was fueled, receiving a total of 44.9 gallons from the fuel truck.
There were no reports received of fuel quality issues with any of the other fueled airplanes.
- Drain Test - An exemplar PA-32-260 (according to the Piper representative to the investigation, the fuel system is the same for the -260 as the -300) was utilized to attempt a comparison with the approximately 1-foot the fuel stain seen on the ramp after the preflight inspection.
After an initial 1-2 second initial draining of the fuel from the exemplar airplane, there was about a 1-foot stain on the asphalt underneath it.
Due to the amount of fuel to be drained, subsequent attempts were drained into a calibrated beaker with stopwatch timings for each attempt, and the fuel was then returned to the airplane.
For 6 seconds of draining, the quantity averaged about 130 ml per draining, and for 12 seconds of draining, the quantity averaged about 260 ml per draining.
Pour tests were then made utilizing water, resulting initially in about a 1 ½-foot puddle for each 130 ml pour, and about a 2-foot puddle for each 260 ml pour.
After about 10 minutes, the puddles had expanded significantly more, but in irregular shapes.
Noted, however, was because of possible differences, such as slope and surface roughness between the test and the prevailing conditions at HKS, an exact comparison could not be made.
Autopsies were conducted on all occupants at the Mississippi State Medical Examiner's Office, Jackson Mississippi, where cause of death was determined to be "inhalation of products of combustion, aircraft crash." The Medical Examiner also confirmed that the occupant of the left front seat was the ATP.
Toxicological testing was subsequently performed by the FAA Forensic Toxicology Research Team, Oklahoma City, Oklahoma, where it was determined that all three occupants had elevated levels of carbon monoxide in their blood.
The ATP had no evidence of drugs in his system.
On October 10, 2012, at 1630 Coordinated Universal Time (UTC), a Sikorsky S-61, Brazilian registration PR-HRU, experienced a loss of power in the number one engine and performed a single-engine landing to Carauari Airport, Carauari Municipality, Brazil.
The flight was operated by HRT.
The two pilots onboard were not injured.
According to information provided by the government of Brazil, helicopter was on final approach for landing when the number one engine experienced a loss of power.
The engine temperature began to increase, and the pilots performed an emergency shutdown.
The helicopter landed without incident.
The investigation is under the jurisdiction of the government of Brazil.
Further information can be obtained from:Aeronautical Accident Prevention and Investigation Center Investigation DivisionSHIS – QI 05 – VI Comar, Brasilia-DF, Brazil 71.615-600Tel (55-61) 3364-8838, Fax (55-61) 3365-1004dac.saai@cenipa.aer.mil.br This report is for informational purposes and contains only information released by the Government of Brazil.
The pilot of the tailwheel-equipped airplane reported that he lost directional control upon touchdown on the runway.
The airplane ground looped to the left, and the leading edge of the right wing dipped and contacted the runway.
The airplane then came to rest upright.
The airplane sustained substantial damage to the right-wing rear spar and right aileron.
The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation.
The automated weather observation system located at the airport reported that, 26 minutes after the accident, the wind was from 250° at 11 knots, gusting to 17 knots.
The pilot landed the airplane on runway 24.
The pilot's failure to maintain directional control during landing in gusting wind conditions.
The pilot was departing in tailwind conditions on an aerial application flight from a 1,800-foot-long turf runway with a full payload of fertilizer.
The pilot stated that the engine lost power during initial climb and that he had insufficient time to dump the payload before impacting a pond off the end of the runway.
Examination of the engine revealed no anomalies that would have precluded normal operation.
According to the airplane manufacturer's calculations, the calculated takeoff distance given the conditions present at the time of the accident exceeded the runway length available; however, the airplane's performance specifications were not available in the POH, which precluded the pilot from conducting performance calculations before takeoff.
It is likely that, as the airplane neared the end of the runway, the pilot lifted the airplane off the ground prematurely and attempted to climb at a steep attitude, which exceeded the airplane's critical angle of attack, which resulted in an aerodynamic stall.
The National Transportation Safety Board determines the probable cause(s) of this accident to be:An exceedance of the airplane's takeoff/climb capability, which resulted in a stall during initial climb at an altitude that was too low for recovery.